The Ashburton had a small crakshaft problem. They started the engine with water in one, as I remember, unit. Result, the engine had the unit twisted 13 deg and the result of effects on the rest of the engine. Engine BW fourstroke. They dragged out from the wharf and left her sitting on the pick at Numeau.
I was one of three who flew from the UK to help bring her back. Metalex (?) from nz also joined the ship. The patched every head while in Fiji, then we spent 29 days crossing the pacific to Panama, where all new heads were put on. We broke day every day, interesting, it pn;y broke down when we were trying to sleep. Liverpool, we were not alowed to stop the engine until we had tigs on. Emptied then down to the Tyne where there pulled half the engine out to line it up. 3 months later, they haded he over the Manners. Al least they seemed to have a large number of fitters, along with the engineers whenthey took over.
Jim B